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cleat

Yet another foot control fabrication

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cleat

I am making a foot control kit for myself based on Matt's design as he appears to be out of the production of this.

None of these parts have been actually tried yet.

The 416H that I just brought home will be my test mule.

 

First on the agenda is the self centering bracket.

Plate has been cut to size then the two holes were drilled.

1293358090_Autocenterleverbluelayoutdyeapplied2.JPG.ed5741b157c6a7dae4b78982ce01880a.JPG

plate has been scribed.

423017873_AutocenterleverscribedforVnotch2.JPG.e673ba6982f3c8b4f874c80719f2fd21.JPG

V notch cut out.

474629673_AutocenterleverVnotchcutout2.JPG.af8968a4e303bfad18be11ae431888b7.JPG

Relief cut into bottom for clearance.

1142623840_Autocenterleverbottomrearcornerreliefcut1.JPG.2562ff3a59f3b34d0b5ccc1c1e162703.JPG

 

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cleat

Cam pivot lever has been cut out and drilled.

1036323430_Campivotlever.JPG.5b9ada03d550993014664c5867d55985.JPG

 

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cleat

Foot pedal adapter plate made up.

Plate cut to size.

932206014_Platecuttolengthanddyeapplied.JPG.0936a9ae1e3c2a9f47e153ecdea63d6e.JPG

Plate scribed and center punched for holes.

1931926620_Platescribedtoshowholecenters.JPG.cf48cfd45c508f7d13b75da4c47b45f3.JPG

746923413_Plateholelocationscenterpunched.JPG.11ea74b420ff9ed96ad55dec14fadc1f.JPG

Plate put into drill press then holes are drilled.

918558555_Platesetupindrillpress.JPG.17bd1204dbd45f3ee949b8a414c4d9e0.JPG

112442779_0.125holesdrilled.JPG.1dc8956b3b7bed28279054fe2ec4b979.JPG

1274690880_0.25holesdrilled.JPG.82d327db393766212b144e54257b1dbb.JPG

166809326_0.375holesdrilled.JPG.f1b7d2d78b147a9b09c086c97f78efc5.JPG

2006206973_Drillpresssetuptodrill1.25centerhole.JPG.bc6beed9fecd59185fd9ee3b5af6679b.JPG

129553383_Plateholesdrilledanddeburred.JPG.c0b879f6e72b68e919abab93c0e152eb.JPG

 

Holes de-burred.

1885427134_Plateholesdrilled.JPG.135f2223d8ec28d4f940fdf9bd3686a9.JPG

 

Plate mounted to pedal.

1084161278_Platemountedonbrakepedal1.JPG.361698fe27d465c84e986489cc978ad4.JPG

1830859851_Platemountedonbrakepedal2.JPG.519ff4d689b72614ea31c86872bd015b.JPG

790636441_Platemountedonbrakepedal3.JPG.e08149945f3725f2ae49b7eed98ad565.JPG

 

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cleat

Control rod made up.

Rods were roughly cut to the proper length then the first bend was made.

1331872798_Firstbendcomplete1.JPG.2d9ed2f9ad9d0e2bb2461779e3520af1.JPG

Second, third and fourth bends made.

907027920_Secondbendcomplete2.JPG.4ec4b13c4e66aaf870d6ec6cf2c0f837.JPG

1536615669_Thirdbendcomplete1.JPG.9bbaf3027117ac3d0cba2484b3786d17.JPG

383330076_Fourthbendcomplete2.JPG.95c8603ff523e9138c1d7a30b8a13422.JPG

 

Rod drilled for the retaining cotter pin and clip.

1939039469_Roddrilled1.JPG.462cd154d006d1b6c98b9649cbf3ee52.JPG

 

End of rod threaded 3/8" NF for the heim joint to screw on.

495903074_RodthreadedNF1.JPG.6030103df5b2f3d02578db278bb1b8f3.JPG

 

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peter lena

@cleat    nice job on that  ! also with all the combined irregularities  , that heim joint  will  help  that work with ease . anytime  dealing with   linkage difficulties , regularly firm up  entire  function , and heim joint finish it  , typically makes it work  without effort , pete 

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cleat

Reverse pedal made up from angle iron cut and bent.

378582170_Reversepedal1.JPG.2981775e53d252212bbc8ea49516d6ec.JPG

333945966_Reversepedal2.JPG.90ec330b05265815f96aefb4e742a8cd.JPG

367550405_Reversepedal3.JPG.a716b6b2910904dd6d20509501fe8fd4.JPG

2117065311_Reversepedal4.JPG.e69456a35cfda13f2dc6b389fc13ca1e.JPG

 

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Wayne0

Watching this!!

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cleat

416H is ready to be used as a test for this foot control.

Shift plate screws and plate itself removed.

2022977117_Shiftcoverplateasfound.JPG.72099b6cda31ba85ab6b4290f20b912b.JPG

 

Right side cover removed.

454840096_Rightsidecoverasfound.JPG.083225768302318cb633b2c1a9decdcc.JPG

837722198_Rightsidecoverremoved.JPG.5137bce2f47d543f223e91417f359e68.JPG

 

Using a 5/32" pin punch to drive out the roll pin in the parking brake knob. (If this was an earlier model this step can be skipped).

487757642_Latemodelparkingbrakeknobasfound.JPG.5bc658768888d6d1dad250bb775fd8a9.JPG

1381956746_5-32pinpunchusedtoremoverollpin.JPG.dfab3f91450bdbb4cf3a426183c61ba1.JPG

1592368153_Latemodelparkingbrakeknobremoved.JPG.f11cf7b60037efa478b1a960ae336dd1.JPG

 

Left side cover can now be removed.

231595125_Leftsidecoverasfound.JPG.0e288791cb24a1a369d0fd365e455608.JPG

1630320111_Leftsidecoverremoved.JPG.0b4a5bc2406983389ff56073246d9c9b.JPG

 

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cleat

Parking brake lever can now be removed mainly for a little more room to do the next steps.

145863034_Parkingbrakeleverreadytoremove.JPG.4b5c0974f392db9a3e8ec19b534df52f.JPG

1828914201_Parkingbrakeleverremoved1.JPG.359c212d1e5340ab66a00da4dbea6185.JPG

243087509_Parkingbrakeleverremoved2.JPG.a5acd70202bdf252e84415b6cc78c432.JPG

 

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cleat

Control rods can now be unbolted from the cam.

590089490_Controlrodsasfound.JPG.6d87a8032ec1c4f1426eb5e1324c6007.JPG

917482477_Controlrodsunbolted.JPG.3e408274d5141358c2a9d7ae031eae62.JPG

 

E clips can now be removed from the control block pin by removing the inside one first then sliding the cam over on the pin and removing the second clip.

1123538138_ControlcamEclipasfound.JPG.a4d5c712f4d0a4176e6380640548e8c3.JPG

2025556957_ControlcamEclipsremoved.JPG.a6f9ea83a32f30cc94feb9e7fba3f34a.JPG

 

Remove the bolt holding the control block pivot pin then pull the pin out and lift the control block out.

954785730_Controlcampivotpinretainingboltasfound.JPG.374c76772ae5c6b81026e6bf75cfc28d.JPG

1290021533_Controlcampivotpinremoved.JPG.e9e211ea2c6d064b1c2fb0ec3db1cdd3.JPG

1418324431_Controlcamremoved1.JPG.d165b1fb52904994c8a2a3257e979ea7.JPG

3774543_Controlcamremoved2.JPG.f6e1c650785cb737c77ecb8bee4e2c30.JPG

 

Control block is now ready to be drilled for the self centering bearing bolt.

1668442250_Controlcamreadytobemarkedfordrilling.JPG.3cba399b7d76880ce4e36948844cc29c.JPG

666298786_Controlcamscribedfordrilling1.JPG.1b7d0971775072b8cc162ed0664fd236.JPG

967208174_Controlcamscribedfordrilling2.JPG.a8d9fb5b7683d0e9183309e042ffea7e.JPG

1034793964_Controlcamcenterpunchedfordrilling.JPG.740befbd2aa19a9932f77115ee176f96.JPG

1845922287_Controlcampilotholedrilled.JPG.8cf189052ab2c8b8371fdabe7c757c36.JPG

1874757299_Controlcam0.25holedrilled.JPG.1f26514e98edf281abe7850aab497579.JPG

Here are the measurements for the hole.

1190256604_Controlcammeasurementsfordrilling.JPG.54309ee14cc6491040ffca83568531de.JPG

 

Control block is now ready to be assembled.

373459280_Controlcamassemblyreadytorassembly.JPG.acea147830352927af80926a5853420e.JPG

 

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cleat

Self centering bracket bolted to the angle iron support.

Note the 1/4 x 1" bolt, three 1/4" flat washers and a 1/4" nyloc nut used in the assembly

Tighten the nut until the bracket and angle iron pivot smoothly but with no extra play.

130947135_Selfcenteringbracketandangleboltedtogether1.JPG.a3e4cfa18dbb3d55f42957baa8af7636.JPG

691850377_Selfcenteringbracketandangleboltedtogether2.JPG.0242de12f3add3bf32b199456ed73d35.JPG

733457523_Selfcenteringbracketandangleboltedtogether3.JPG.5dcdcaabd5c16d673a78438cad7eb03b.JPG

1493633201_Selfcenteringbracketandangleboltedtogether4.JPG.b2b652f17b6a4411103c861206e89674.JPG

1541695300_Selfcenteringbracketandangleboltedtogether5.JPG.5db1a7eee0be40a8cee1ff51a005a475.JPG

 

Mark the hoodstand for drilling a 3/16" hole for the self centering spring to hook into.

This hole is 1-3/4" from the right side and 1/4" down.

1819641428_Hoodstandreadytobedrilledforspring1.JPG.b7cbc42b37f5e422bd7db8f09e283242.JPG

111860592_Hoodstandreadytobedrilledforspring2.JPG.84de675bd68119a181560fea36e17422.JPG

140036910_Hoodstandreadytobedrilledforspring3.JPG.ec7a309b6854974b87fcde0b88c7c823.JPG

698096676_Hoodstanddrilledforspring.JPG.4c98d6ea9c0e1117771a93fd47bcbebd.JPG

 

Remove these two bolts that fasten the hoodstand to the frame and reuse them to bolt in the self centering assembly.

881952337_Hoodstandassemblyboltstoberemoved.JPG.cc4d4094928036612a55c74f656bdb4f.JPG

1201452705_Selfcenteringassemblyboltedin1.JPG.432713f644e57e8a861170c85f3f8885.JPG

1711243903_Selfcenteringassemblyboltedin2.JPG.504d78174ac122288333b94dc9ebe362.JPG

1782229927_Selfcenteringassemblyboltedin3.JPG.a841d5bfc5ee5f736421a9e24f546693.JPG

 

 

Edited by cleat
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peter lena

@cleat   https://www.amazon.com/Super-Lube-52004-Lightweight-Translucent/dp/B00175VGUA/ref=sr_1_3_pp?dib=eyJ2IjoiMSJ9.iLC8Z6DqibaMBjuJ9vu0Yk-M-i  regularly addd this to any  questionable area , especially lever / linkage areas / cables , swing bushings work without effort , also fends off surface rust . pete 

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cleat

Self centering bearing ready to be installed onto the control cam.

848991948_Selfcenteringbearingreadytoinstall.JPG.5aa64b41eaa9ce80c0ba885a273530a0.JPG

 

Bearing installed and nut tightened. Note the orientation of the washers.

Bearing should turn freely when installed.

1965830796_Selfcenteringbearinginstalled1.JPG.b1f97558baf4ed52c87a57cec021d638.JPG

316693260_Selfcenteringbearinginstalled2.JPG.2c13edce9137ef061f399e9e6e0b7ec7.JPG

167525089_Selfcenteringbearinginstalled3.JPG.bab9cdd3a4bb2e2b514b966a043e05a1.JPG

 

Control cam assembly and pivot lever ready to install.

The lever should slide on to the pin easily so it can move without resistance once fully installed.

If it seems tight then the pin may need to be sanded smooth.

1820339755_Controlcamassemblyandcampivotleverreadytoinstall.JPG.931950555285df67be64b7e3832ba917.JPG

 

Control cam inserted into proper location and it's pin partly installed.

878325760_Controlcamandpivotrodpartlyinstalled2.JPG.d5c51c08b624fa4d8e0184d51849d50e.JPG

1047071089_Controlcamandpivotrodpartlyinstalled1.JPG.fadaf84de718f9e2af7ba24770c44c9a.JPG

 

Control cam pivot lever installed onto pin long side up.

1393897081_Controlcampivotleverslidontorod.JPG.5bc4f93eaaecc1f733d6f0c587a0580b.JPG

 

Pin fully inserted and bolted into place.

Left side E clip installed then control cam moved over tight to that clip.

Right side E clip installed.

Control rod bolted up which also holds the pivot rod in place.

311728719_Controlcamandrodassembledalongwithcontrolrod.JPG.da174ee604da034b362a9786cbb43cbc.JPG

 

Speed control cam (under seat) tension nut (the middle one with the large flat washer) backed off a turn or two until the cam can move freely side to side but not lift up and down.

1877100120_Speedcontrolcamtensionnutbackedoffaturnortwo1.JPG.908328dbf60f0fad662b0cb36a5c56e9.JPG

1208802570_Speedcontrolcamtensionnutbackedoffaturnortwo2.JPG.74239d863c38bed18884916af92434c8.JPG

 

You now should be able to move the control cam from front to back where the control rod is bolted on fairly easily.

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ebinmaine

Excellent work as usual @cleat

 

Top notch documentation.  

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cleat
1 hour ago, ebinmaine said:

Excellent work as usual @cleat

 

Top notch documentation.  

Thanks Eric.

 

Pardon the dirty tractor, I am documenting it as found for now and it will come apart for a thorough cleaning and possible restoration later..

 

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rick

Very nice, cleat!

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953 nut

@cleat, as usual you have done an outstanding job of documenting your project.           :text-thankyouyellow:

I was wondering if an automotive shifter cable assembly could be used in place of the rod pictured below?

558178123_shiftcable.jpg.0e14aeeb014746f5b328ab14eac04646.jpg

495903074_RodthreadedNF1.JPG.6030103df5b2f3d02578db278bb1b8f3.JPG

 

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cleat

It might work so long as you can push and pull on it.

 

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953 nut
33 minutes ago, cleat said:

It might work so long as you can push and pull on it.

 

That was my thought, ridged linkages for automotive automatic transmissions haven't been used in years      :confusion-confused:    Why not on a Wheel Horse?

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cleat

This machine is a very late model so it has the padded footrests which have no room for the foot pedal.

This is now unbolted and removed.

1135559886_Verylatemodelfootrest1.JPG.761ba7ee15e7df2b515169a4c154b954.JPG

2073969723_Verylatemodelfootrest2.JPG.66ec65dcb5425daafbd1d603fac24e13.JPG

 

Since I have an earlier model footrest I will show the difference.

1621888261_Standardfootrest1.JPG.cbc0da1a00e1dce33c199bfa50db042e.JPG

441059052_Standardfootrest2.JPG.774e25ab9684768b5327df88e3b1a2c0.JPG

 

Control rod, cotter pin, washers, and hairpin clip ready for installation.

1724753340_Controlrodwashersandclips1.JPG.e89e4df8218a52b2dd68b5274e824900.JPG

781052498_Controlrodwashersandclips2.JPG.ade82b9694f8a54bcab4ff63ecaf042a.JPG

 

Cotter pin installed just barely bent for now as this will be coming back apart for paint.

630617322_Controlrodcotterpininstalled.JPG.8af55f415a95fae17e0e2ae2f8ff0964.JPG

 

Control rod heim joint and jamb nut ready to assemble.

1461585781_Controlrodheimjointreadytoinstall1.JPG.6dc6db2f2757933210db266d7d59c47c.JPG

1300083554_Controlrodheimjointreadytoinstall2.JPG.c0c56967a9fffad21fcf0967552643f2.JPG

692165481_Controlrodheimjointlooselyinstalled.JPG.fda66fd6b4665dc84454f21d167b267b.JPG

 

Control rod being inserted into tractor.

849214797_Gettingreadytoinstallcontrolrod.JPG.26974e7bc6b417ea3f26e4d4d21c15ef.JPG

1290182561_Controlrodslightlyinserted.JPG.3f0e16f177a1fa7e50baa526d179119f.JPG

462527626_Controlrodmostlyinserted.JPG.f8ce896d02d1c267412304204a2bb2c4.JPG

1193999532_Controlrodinstalled.JPG.6d878565fe12872b38d1a1549ea57363.JPG

 

Install a washer onto control rod then insert into cam pivot lever bottom hole.

148804312_Controlrodinstalledintocampivotlever1.JPG.2b3ec7202ea00d41690462373587c661.JPG

 

Now install a washer and then the hairpin clip onto the control rod.

I use long needle nose pliers to install the clip.

894844381_Controlrodinstalledintocampivotlever2.JPG.cfd9842d9a9c54f07e892c8c2051ad83.JPG

1230757545_Controlrodinstalledintocampivotlever3.JPG.a2f120751edd272105ddad0ed0ae4cd5.JPG

749153566_Usinglongneedlenoseplierstoinstallcontrolrodclip.JPG.07f69a50f916386abf40a13497b42f8c.JPG

 

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cleat

Foot pedal ready to have reverse pedal and plate bolted on.

Standard nuts are used for now but nyloc nuts will be used on the final assembly after paint.

2051438670_Footpedalreadytoassemble.JPG.da9140c487f1802d7ba9467b30efce19.JPG

 

Reverse pedal and plate bolted on.

1658597365_Footpedalassembled1.JPG.d88387b4306a8427dbe059d2899e0ad6.JPG

32556414_Footpedalassembled2.JPG.73e2fed6acb5746be781c161e395d0b7.JPG

2056712548_Footpedalassembled3.JPG.df135bde94b6fb7145f369d4d92022d8.JPG

 

Pedal installed onto tractor then the retainer is installed and tightened to hold pedal onto the shaft.

Heim joint is bolted to the pedal plate and nut tightened.

Note the 3 washers used to keep the heim joint free moving.

26473217_Heimjointboltedtopedalplate3.JPG.3b4e7d635e3126897f865c533c4f30b8.JPG

502679801_Heimjointboltedtopedalplate1.JPG.2c5ed92ed60948e00989a1edf355f316.JPG

1919443218_Heimjointboltedtopedalplate2.JPG.2ebebb3e68d874b6de25091ec09a2a8b.JPG

863737269_Heimjointboltedtopedalplate4.JPG.0f6f16308af16c67189f591d3d6c0360.JPG

 

Foot rest loosely sat into position then the foot pedal was pushed to full reverse.

At this point the reverse pedal should sit just up a bit (1/4" or so) from the foot rest to ensure you get full reverse speed.

If it is too high or it just hits the footrest then it's height can be adjusted by screwing the heim joint in or out on the rod as required.

Fully tighten the heim joint to foot pedal plate each time to ensure an accurate measurement.

1827762166_Footrestlooselysatinposition.JPG.1eb045deeb77f594a0bb2109bb2d5c1f.JPG

1720134435_Adjustlengthofcontrolrodheimjointuntilreversepedalsitsupjustalittlefromthefoorrestwheninfullreverse.JPG.687e214e4fb4bd59d2d0ce2638ad5937.JPG

 

Foot pedal in neutral position.

812116109_Footpedalinneutral.JPG.cd2ddf78689d395e4875373f653407f5.JPG

 

Foot pedal in full forward position.

308417864_Footpedalinfullforward.JPG.e9b4ed73a67ac2704ffe66b1f4cdf332.JPG

 

Auto center spring.

361455557_Autocenteringspring1.JPG.cfa6454332fb1a818577e71e49a8a122.JPG

973527663_Autocenteringspring2.JPG.81096a6f374107556d0d8b656fa52ede.JPG

 

Spring hooked into auto center lever.

1436698245_Springinstalledontoautocenterlever.JPG.d21675e9171c7561059fb4ef8f7ce7ba.JPG

 

Spring now gets hooked into the hoodstand plate where the hole was drilled earlier.

668287270_Springhookedintohoodstandplate1.JPG.63d7cf961cb97b55f7324b9c601144b7.JPG

785253501_Springhookedintohoodstandplate2.JPG.5c4de40aca2f6ef580cc47f310c58f73.JPG

 

Footrest bolted down.

284811244_Footrestbolteddown.JPG.283477b4f3f09ede5427da45306e9f7a.JPG

 

Control shaft heim joint jamb nut tightened.

1331793595_Controlrodheimjointjambnuttightened.JPG.c1c4969807c77afdf9850ca87c3f0de8.JPG

 

 

 

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cleat

Parking brake lever installed.

1957354392_Parkingbrakeleverreadytoinstall.JPG.4e66f9dc7bfd85dc16c57ad694ca89a7.JPG

450325932_Parkingbrakeleverinstalled.JPG.3b80c4945038b715a42a8998726e7597.JPG

 

Right side cover and shift covers installed.

424900650_Rightsideandshiftcoversinstalled.JPG.3d89f81b8f9bbe19021477c1f0b23d1a.JPG

 

Left side cover and parking brake knob installed.

1047735659_Leftsidecoverandparkingbrakeknobinstalled.JPG.07fdc70134a732914ca1586876ce284b.JPG

 

The foot pedal adapter plate needs to be trimmed just a bit.

It does not make contact but it is really close.

1035013713_Foodpedalplatetrimmingrequired1.JPG.29563604f3fbba728aba90a902ad8e6d.JPG

1939641462_Foodpedalplatetrimmingrequired2.JPG.818a014ef8b519f08c2f6b23ae515a91.JPG

 

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cleat

Rear end of tractor jacked up.

776821465_Jackrearwheelsoffground.JPG.f1199e18536be015b5916a4923aa4ec6.JPG

 

Now the engine can be started and ran for a few minutes then increase to full throttle.

Note: the neutral safety switch will need to be satisfied for the engine to start. I just made sure the old column shifter was in the neutral position.

Rear wheels should not be turning.

Push foot pedal forward then release pedal.

Wheels should stop.

Push foot pedal reverse pedal down then release.

Again, wheels should stop as soon as pedal is released.

If wheels do not stop rotating then adjust eccentric cam at Hydro as per the attached service manual.

You will need a 1" wrench for the eccentric and a 1/2" socket or wrench for the eccentric bolt.

15798483_Adjusteccentricuntilwheelsdonotturn.JPG.6d0219dec36b25ddf624ce6f022a582a.JPG

 

Wheel horse 520H service manual.pdf

 

When a satisfactory neutral has been obtained then remove the jack.

 

 

 

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cleat

When this tractor gets it's overhaul I will be removing the column shift lever and the safety neutral switch

 

I feel safe doing this because the tractor now reverts to neutral unless you are pushing on the foot pedal.

 

This foot control shows installation with a column shift tractor.If you have a motion control that is between your legs then you will be unbolting and removing the motion control lever from the motion cam.

The neutral safety switch is mounted on the shift plate and will need to either have the switch taped down or the wires jumpered in order for the tractor to start (purple and light blue in the case of a 520).

1311583631_Floorshift.jpg.36c6ac7ec1e4bd7a310b2660b89468e8.jpg

 

floor shift.pdf

 

Important....do not run the tractor with the neutral safety switch bypassed until you are absolutely sure the tractor returns to neutral with the foot pedal released.

 

Another option I have been toying with is wiring the parking brake switch into the start circuit so tractor will only start with brake locked on.

Edited by cleat
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SylvanLakeWH
3 minutes ago, cleat said:

 

I feel safe doing this because the tractor now reverts to neutral unless you are pushing on the foot pedal.

Curious... not a hydro guy, but I assume need for adjustment periodically or if it comes out if adjustment, should a safety switch not be maintained?

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